PECO ENERGY CO
8-K, 1997-01-30
ELECTRIC & OTHER SERVICES COMBINED
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                                    FORM 8-K





                       SECURITIES AND EXCHANGE COMMISSION




                              Washington, DC 20549

                                 CURRENT REPORT



                Pursuant to Section 13 or 15(d) of the Securities
                              Exchange Act of 1934




                        Date of Report: January 30, 1997



                               PECO ENERGY COMPANY
             (Exact name of registrant as specified in its charter)



                         PENNSYLVANIA 1-1401 23-0970240
                       (State or other (SEC (IRS Employer
                   jurisdiction of file number) Identification
                             incorporation) Number)




              230l Market Street, Philadelphia, Pennsylvania 19101
               (Address of principal executive offices) (Zip Code)



               Registrant's telephone number, including area code:
                                 (215) 841-4000



<PAGE>


Item 5. Other Events

On January 29, 1997,  Public  Service  Electric and Gas Company  (PSE&G) and its
parent, Public Service Enterprise Group Incorporated filed the following Current
Report on Form 8-K concerning Salem Nuclear Generating Station (Salem), operated
by PSE&G:


"PSE&G - Nuclear Operations
- ---------------
On January 29,  1997,  the  Nuclear  Regulatory  Commission  (NRC) held a public
meeting and identified  plants placed on the "NRC Watch List",  including  Salem
Units 1 and 2, which were identified as Category 2 plants.  In its press release
issued following the meeting, the NRC stated:

"The staff informed the Commission that the decision to place the Salem units on
the Watch List was not based on any recent performance  problems or decline; the
staff believes that Salem's efforts to achieve needed improvements are correctly
targeted and the NRC is satisfied with the licensee's overall approach. However,
the staff noted that Salem should have been placed on the Watch List  previously
because of Salem's past safety  performance.  The staff also  indicated that the
agency increased its attention and resources at Salem  commensurate with a Watch
List plant. Finally, the staff concluded that,  notwithstanding the improvements
at Salem, it would not have been removed from the Watch List at this time had it
been  previously  identified  because it has yet to demonstrate a period of safe
performance at power".

The NRC has three classifications of facility monitoring.  A Category 3 facility
is  one  which  is  having  or  has  had  significant  weaknesses  that  warrant
maintaining the plant in a shutdown condition until the licensee can demonstrate
to the NRC that adequate  programs have both been established and implemented to
ensure  substantial  improvement;  full NRC approval is required for restart and
the NRC  will  monitor  closely.  A  Category  2  facility  is a  plant  that is
authorized  to operate but that the NRC will  monitor  closely;  although  being
operated in a manner that adequately  protects public health and safety,  plants
in this category are having or have had  weaknesses  that warrant  increased NRC
attention;  a plant  will  remain in this  category  until the  licensee  either
demonstrates a period of improved performance,  or until a further deterioration
of  performance  results in the plant  being  placed in Category 3. A Category 1
facility is a plant that that has been removed from the Watch List.

More fully  describing  this NRC action,  on January 27, 1997,  the NRC sent the
following letter to PSE&G:


<PAGE>



                                  United States
                          Nuclear Regulatory Commission
                                Washington, D. C.



January 27, 1997

Mr. E. James Ferland
Chief Executive Officer
Public Service Electric and Gas Company
80 Park Plaza
Newark, NJ 07101

Dear Mr. Ferland:

On January 14, 15, and 17, 1997, NRC senior managers met to evaluate the nuclear
safety performance of operating reactors,  fuel facilities,  and other materials
licensees. The NRC conducts this meeting semiannually to determine if the safety
performance  of various  licensees  exhibits  sufficient  weaknesses  to warrant
increased NRC attention.  At the January 1997 Senior  Management  Meeting (SMM),
the Salem and Hope Creek Generating Stations were discussed.

In our letter of January 29,  1996,  James M. Taylor,  the former NRC  Executive
Director for  Operations,  advised you that at the January 17-18,  1996 SMM, NRC
senior managers concluded that recent trends in performance at Hope Creek raised
sufficient concerns that we believed it would be appropriate to meet with you to
discuss  these  concerns.  In that letter we also stated that  resolution of our
performance  concerns at Salem remained to be demonstrated through sustained and
reliable operations.

At the January 1997,  SMM the  discussion  regarding  Hope Creek  considered the
additional  insights gained from our monitoring of plant  performance  since the
January  1996  SMM.  Based  on  these  discussions  it was  concluded  that  the
corrective actions you are taking have been effective in addressing our concerns
regarding  adverse  trends  in  performance  at Hope  Creek.  A  summary  of NRC
discussions related to Hope Creek follows:

Steps taken by management to address both human performance and equipment issues
over the past year have resulted in an overall improvement in plant operations.

Management  has  consistently  exhibited  a  conservative  approach  to decision
making.  Progress has been made in  communicating  higher standards and lowering
significantly the threshold for  identification  of problems.  Numerous staffing
changes and an extensive  training and  requalification  initiative  have led to
improved control of plant activities by operators. This is significant since the
negative trend  discussed in the January 1996 SMM was most notably  evidenced by
several  significant  events where  operators  failed to properly  control plant
evolutions. Overall personnel error rates have declined significantly.

The station is well along in  addressing  previously  identified  problems  with
technical  specification  and  surveillance  procedure  discrepancies.   Overall
material  condition  of the  plant  is good as  illustrated  by  improved  plant
operating  performance.  This improvement  stemmed, to a large degree, from work
accomplished during an extended outage completed in early 1996.  Maintenance and
engineering  backlogs are well  understood and prioritized but they constitute a
continuing  challenge  to the  station.  Continuing  attention is also needed to
improve  operator  staffing  levels  which  were  reduced  somewhat  during  the
station's operator requalification initiative.

The senior  managers  also  discussed the Salem  facility.  As described in more
detail in the following paragraphs,  Salem was designated as a Category 2 plant,
not due to any performance  problems or decline during this  evaluation  period,
but due to a change in senior  management  judgment as  described  in the fourth
paragraph below, A summary of NRC discussions related to Salem follows:

Both Units I and 2 were shut down to  address  significant  equipment  and human
performance  problems in mid-1995.  An NRC Confirmatory  Action Letter issued at
the time established actions required before restart of the Units.

A strong  management  team has been assembled by PSE&G; it has been in place for
most  of  the  outage.  A  much  lower  problem  reporting  threshold  has  been
established  and  management  has been  aggressive  in  addressing  root causes.
Significant  staffing changes have been made.  Operations and maintenance staffs
have completed extensive training and requalification programs to both reinforce
fundamental skills and establish higher safety standards.  Steps have been taken
to  strengthen  station  self  assessment,  corrective  action and work  control
processes.  As a result,  the number and  significance of personnel  errors have
declined.  Operators  have  demonstrated  improved  ownership  of the  plant and
conservative decision making.

The  outage  scope  has been  extensive.  Numerous  plant  components  have been
refurbished or replaced with the more reliable equipment in both  safety-related
and  balance-of-plant  systems.  Operator  work-arounds are being  addressed.  A
comprehensive,  pre-startup  test program is underway to assure  repair work has
been effective.  Engineering  organizations  are providing  stronger  support on
equipment and design  issues as evidenced by  completion  of a recent  licensing
basis conformance review.

The senior managers  thoroughly  discussed  current  activities at Salem and the
basis for past SMM decisions. The conclusion was that the scope and depth of the
problems  that  existed  at  Salem  prior to the dual  unit  shutdown  warranted
categorizing  it as a Category  2 facility  indicating  need for  increased  NRC
attention.  Past decisions  regarding  Salem's status were influenced by current
licensee management's  recognition of problems and efforts being made to address
them. As a practical matter, given the extent of these problems and the scope of
activities,  the agency  increased its attention to Salem and applied  resources
commensurate  with a plant in a Category 2,  status.  As a  consequence,  senior
managers  reviewed Salem  performance using the Category 2 plant removal matrix.
The managers  concluded,  notwithstanding  the significant steps being taken and
results  achieved to date,  Salem would not be removed from Category 2 status if
it had previously been  categorized as such. A key  consideration in the removal
matrix is assessment of plant and integrated station  performance at power which
has yet to occur.

In summary,  the  decision  was made to  recognize  that Salem  should have been
placed on the watch list  previously  and that it would not have been removed at
this point. As such,  Salem is being classified as a Category 2 facility at this
time.  This  classification  is not  intended to suggest that  licensee  actions
underway at Salem to achieve needed improvements are incorrectly  targeted.  NRC
is  satisfied  with the  overall  approach  and will be  monitoring  closely the
progress to achieve the planned improvements.

An NRC Commission meeting,  open to the public, has been scheduled to be held in
the Commissioners' Conference Room in Rockville,  Maryland, on January 29, 1997,
at 10,00  a.m.  to review  the  results  of the  latest  meeting  of NRC  senior
managers. Mr. Hubert Miller, the Region I Regional Administrator,  has discussed
the bases for our  conclusions  with regard to Hope Creek and Salem with members
of your staff.

If you have any questions regarding this matter, do not hesitate to call me.

                                                              Sincerely,
                                                       HUGH L. THOMPSON, JR.
                                                       Hugh L. Thompson, Jr.
                                        Acting Executive Director for Operations

Dock Nos:
50-272
50-311
50-354"




<PAGE>


                                   SIGNATURES




Pursuant  to the  requirements  of the  Securities  Exchange  Act of  1934,  the
registrant  has duly  caused  this  report  to be  signed  on its  behalf by the
undersigned hereunto duly authorized.






                                     PECO ENERGY COMPANY


                                      \s\ J. B. Mitchell
                                   Vice President - Finance
                                         and Treasurer






        January 30, 1997






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